1997 Ford F-250
Problem Areas
Complaints Over Time
Recent Complaints
TL* THE CONTACT OWNS A 1997 FORD F-250. THE CONTACT STATED THAT HE WAS INVOLVED IN A CRASH WHERE THE AIRBAGS DID NOT DEPLOY AT THE POINT OF IMPACT. A POLICE REPORT WAS FILED AND AN INJURY WAS SUSTAINED THAT REQUIRED MEDICAL ATTENTION. THE VEHICLE WAS DESTROYED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 278,000.
WHILE TRAVELING ON ARIZONA STATE HWY 87 NORTH FROM PAYSON AS ENTERING INTO PINE ARIZONA I STRUCK A LARGE TRUCK FROM REAR. THIS CAUSED SIGNIFICANT DAMAGE TO THE DRIVER SIDE OF THE TRUCK ACTUALLY BREAKING THE FRAME, PUSHING THE FRAME THRU THE BUMPER AND REQUIRING THE FIRE DEPARTMENT TO UTILIZE THE JAWS OF LIVE AND RELEASING THE STEERING WHEN FROM MY CHEST. INJURIES INCLUDED SKULL FRACTURE, BROKEN FEMUR, CHEST AND HEART CONTUSION. AIRLIFTED TO NEAREST HOSPITAL. LATER FOUND THAT THE INSIDE OF THE STEERING WHEEL APPEARED TO BE POPPED OFF AND WAS HANGING BY A CABLE YET AN AIRBAG WAS NOT PRESENT. TRYING TO FIND OUT IF THE TRUCK WAS ORIGINAL WITH AN AIRBAG. IT WAS A GOVERNMENT STATE OF ARIZONA VEHICLE. *TR
MY WIFE DRIVING VEHICLE AT APPROX. 35 MPH, AFTER COMING OUT OF A SLIGHT CURVE IN ROAD AND SLOWING FOR A STOP SIGN, SHE LOST ALL STEERING CONTROL OF VEHICLE HITTING A GUARDRAIL AND GOING INTO A DITCH. INSPECTION BY AN ASE CERTIFIED MECHANIC REVEALED THAT THE OUTPUT FROM THE STEERING BOX BROKE BETWEEN GEAR BOX AND PITMAN ARM CAUSING A TOTAL LOSS OF STEERING CONTROL. TRUCK IS TOTAL. VEHICLE IS CURRENTLY AT LUCAS CHEVROLET, MT. HOLLY NJ. *NM
REAR BRAKE FAILURE ON NUMEROUS OCCASIONS. FINALLY RESULTED IN CRASH. DEALER COULD NOT FIND ANY PROBLEM. SELF DIAGNOSIS OF RAISING REAR OF VEHICLE WHILE IDLING IN DRIVE WITH REAR WHEELS SPINNING REAR WHEELS COULD NOT BE STOPPED WITH FULL BRAKE PRESSED. NO BRAKING ON REAR WHEELS. DISCONNECTING WIRE TO PROPORTIONING VALVE RESULTS IN NORMAL REAR BRAKE OPERATION. POSSIBLE CAUSE IS EBCM OR PROPORTIONING VALVE.
CONSUMER WAS ENTERING A FREEWAY AT 45-50 MPH WHEN HE TRIED TO STOP VEHICLE AND COULD NOT DUE TO BRAKE FAILURE. *AK
NO DEPLOYMENT OF AIRBAG IN A HEAD ON COLLISION ACCIDENT. DRIVER SUSTAINED INJURIES.
1997 FORD F25. THIS WAS THE SECOND SPARK PLUG TO BLOW OUT OF HEAD. FIRST REPAIR COST $450.00, THIS TIME IT COST ME MY TRUCK, 2 CAMERAS, GPS, LAPTOP COMPUTER AND SEVERAL OTHER ITEMS AS THE TRUCK COUGHT ON FIRE WHEN SPARK PLUG HIT FUEL INECTION RAIL AN STARTED A FUEL FIRE THAT BURNT THE TRUCK TO GROUND. TOTAL LOSS. BURNED MY HANDS TRYING TO SAVE ITEMS IN CAB. HAD A FIRE EXTINGUISHER, BUT HIGH PRESSURE FUEL LINES SPRAYED FIRE TO FAST. MY GIRL FRIEND, HER DOG, AND I HAD 30 SECONDS TO GET OUT. IN 2 MINUTES THE CAB WAS ENGULFED IN FLAMES. I WILL BE DISMANTLING THIS ENGINE AS I AM A MECHANIC AND MACHINIST AND PLAN TO PROVE THERE WERE NOT ENOUGH THREADS SECURING SPARK PLUGS IN THEE ALUMIN UM HEADS. THERE WERE STANDARDS OUTLINED FOR MACHINING THREADS.*AK
WHILE DRIVING 35 MPH AND WHEN VEHICLE WAS GOING AROUND A BEND THE STEERING FAILED TO RESPOND, CAUSING VEHICLE TO CRASH INTO A GUARD RAIL. BOTH MANUFACTURER AND DEALER WERE CONTACTED. *AK
VEHICLE INVOLVED IN CRASH, ENGINE WAS STILL RUNNING AND THE SEAT BELTS DID NOT HOLD.*MR. THE CONSUMER STATED THE OWNERS MANUAL STATED THERE WAS AN AIR BAG IN THE VEHICLE, HOWEVER NO AIR DEPLOYED. *JB *NLM
RIGHT SIDE OUTER TIR ROD END CAME APART. VEHICLE WENT OFF THE ROAD STRUCK A MAIL BOX AND POWER POLE AND LOW VOLTAGE PEDASTEL AND PULLED POWER LINE FROM NEIGHBORING HOUSE. CAUSING DAMAGE TO HOUSE.*AK
WHY IS THE IGNITION SWITCH RECALLED ONLY FOR F-150 PICKUP TRUCKS WHILE THE SAME SWITCH IS IN THE F-250 AND F-350 TRUCKS AS WELL? *AK
CONSUMER WAS TRAVELING AT HIGHWAY SPEED AND WITHOUT PRIOR NOTICE REAR BACK TIRE TREAD SEPARATED FROM VEHICLE. *AK
CONSUMER WAS INVOLVED IN A FRONTAL COLLISION AND DRIVER'S SIDE AIR BAG FAILED TO DEPLOY. PLEASE PROVIDE ANY FURTHER DETAILS.*AK
NO SUMMARY LISTED FOR ABOVE VEHICLE. *AK (TIRESIZE: 235R16)( DOT NUMBER: TIRE SIZE: 235R16 )
NO SUMMARY
VEHICLE WAS INVOLVED IN AN ACCIDENT WHEN ANOTHER VEHICLE ROLLED OVER IN FRONT AND ON TOP OF CONSUMER'S VEHICLE, DAMAGEING THE FRONT BUMPER,/HOOD AN D/LEFT FENDER. UPON IMPACT, BOTH AIR BAGS FAILED TO DEPLOY. DEALER / MANUFACTURER NOTIFIED. SEEKING HELP FROM NHTSA IN THIS MATTER. *AK
AUTOMATIC TRANSMISSION MALFUNCTIONED WHEN VEHICLE WAS IN THE PARK. OCCUPANT GOT OUT OF VEHICLE, AND VEHICLE ROLLED AWAY INTO A LAKE. PLEASE PROVIDE FURTHER INFORMATION AND VIN#. *AK
THE VEHICLE HAS NO ADEQUATE HYDRAULIC FILTER ON THE RELEASE VALVE WITHIN THE STEERING GEAR BOX TO PREVENT VALVE COMTAMINATION AND FAILURE, CAUSING THE STEERING GEAR BOX TO EXPLODE AND TOTAL LOSS OF POWER STEERING WHICH RESULTED IN AN ACCIDENT. CONSUMER HAD IT ANALYZED BY DOUGLAS B. CHISHOLM ASSC. INC WHICH DETERMINED THE DEFECT. PLEASE ATTACH THE ADDITIONAL INFORMATION. *AK
WHILE DEPRESSING THE BRAKES THE VEHICLE CONTINUES TO TRAVEL, CAUSING AN ACCIDENT. DEALER HAS BEEN CONTACTED. PLEASE PROVIDE FURTHER DETAILS. *AK
WHEN INVOLVED IN A CRASH, IMPACT SPEED AROUND 30-35 MPH, FRONT END DRIVER'S SIDE. THE BUMPER WAS PUSHED BACK, WHICH CAUSED THE LEFT FRONT TIRE TO BUST. DAMAGES TOTALLING $6,000 DOLLARS. IN THIS CRASH THERE WAS NO DEPLOYMENT OF AIR BAGS. THE TRUCK IS BEING REPAIRED. *AK
